A bit more driving the Corsair happened today and what a lovely day it was. First it was family trip to Compton Abbas Airfield, and the Corsair struggled up Spread Eagle hill in second gear with a line of traffic behind, but probably glad that I turned off for the airfield. After my son had his flight experience at the airfield I took a scenic route home via the fantastic B3081 that has far reaching views to Shaftesbury and the Blackmore Vale and then a drive down the legendary Zig Zag Hill. The brakes were fine and the tight turns ok.
After some lunch another jaunt took us out to Clayesmore School where I took the opportunity to take some photos against the back drop of the school’s main house. The car ran well and I’m getting used to the flat spot and driving through it. It also keeps up well with the local traffic, except on the big hills! So after three trips the corsair had done 54 miles. More fuel will be required before the next trip out, just in case.
So, once home I had to deal with the soggy carpet (when it got drenched over night last Friday) in the passenger side rear foot well. As per usual, a seized bolt holding the seat fame to the floor sheared so I needed to drill that out and re-thread to fit another bolt (metric though). It was a very good day.
No maidens here, but took the old Corsair for a run with my son as passenger. First it was a stop at the petrol station to put in a couple of gallons and refill the fuel can – just to be sure. The car was a bit lumpy under load but the extra choke dealt with that.
So a nice 34 mile loop of the locale was covered and felt great to be back behind the wheel. The fuel gauge doesn’t work and the temperature gauge kept moving about however the speedo was fairly accurate when compared to the speed app on the phone. The car cruised quite well at 50mph but didn’t like being under load at lower revs and performed better when the choke was eased out. It was a good drive and allowed the car to dry out some more after getting a soaking from Friday into Saturday.
Went to John’s this morning to pick up the Corsair and in typical style it was lashing with rain when I arrived. John’s hospitality was tip top as usual and came with a cup of tea. With the bill paid it was a briefing on how the Corsair would like to be started and warmed up. John had spent some time the previous day fettling the tune on a few trips to Win Green and back. So all was good and it ran well on the trip home which was very wet and the wipers worked well. A bit lumpy and noisey and lots to deal with but I got the Corsair home.
John has had the Corsair since April, with the brief to tune up the carburettor to run better between his better paying jobs. If you go back through the blog threads you will read that it has been something of an epic journey, testing the patience and skills of John and Peter. The work done has entailed the tidying up of the fuel lines and re-positioning the in-line fuel filter after the fuel pump and stripping down the carburettor and using parts from the spare I provided, leading into their nemesis of the ignition and distributor problems and finally getting it through an MOT.
Went to see John today as the Corsair is now up and running very nicely, especially now that it can be tuned properly and has many new ignition components. It has been booked for an MOT on Thursday – just to see if anything more needs doing. Fingers crossed, eh?
H& H Ignition Solutions [website here] delivered as promised a rebuilt and refurbished distributor. It looked like new. I presume my original internals were used but a new body was sourced which was added to the total refurbishment cost. You can see from the photos what a great looking piece of kit it looks like, just hope it performs as well as it looks.
So the new dizzy was passed to John along with a collection of gaskets and an oil filter for the engine re-assembly and hopefully a good starting point for a fresh tune-up.
John and Peter at AJ Restorations had finally got the distributor out. They eventually used an aluminium drift from beneath and persuaded it out, after drilling the alloy body to release it from it’s infernal grip on the cast iron block.
It didn’t look too good but I was assured in a phone call to H&H Ignition in Dudley, Birmingham that they could refurbish anything so long as the internal main shaft was OK along with the cog drive. John also had a contact that may have a couple of spare distributors for future reference, just in case mine was unserviceable.
So that’s it for now. I’ll be taking this little lot up to H&H Ignition on Tuesday (15th Aug) and see what they have to say.
The distributor has been causing all manner of problems for John and Peter at AJ Restorations. It had battery acid soaked into it for a week and it still wouldn’t budge. Heat and brute force with massive grips could not move it, either.
Upon visiting John last Friday (28th July) it has been decided to dismantle the distributor to leave the aluminium shell and then cut the bugger off and then drill out the seized in remains. I have been assured from an ignition specialist that they can rebuild the distributor from the bits I supply.
In all this time, I’ve been trawling Ebay for a replacement but they are all Dizzy’s from V4 Transits or quite pricey only to be rebuilt anyway. The distributor I had (Bosch) is for a Pinto and manufactured in 1976 and will be on Ebay soon.
It will get done, though it’s costing a lot more than first thought.
The Corsair has been with John at AJ Restorations for 2 months now, however my brief to him was to tinker between his bigger paying jobs to keep the costs down, only thinking it would be a carburettor tweak and a few other bits of tuning to get the car running properly. Well, nothing is ever simple. There are problems with the carburettor possibly having the wrong idler needle and jets but the main issue now is that the distributor appears to have seized in its mounting and won’t turn for adjustment.
Visiting John’s today, I got to chat with Peter who helps out twice a week and is Ford trained from the 1970’s so he is quite familiar with the Corsair. However, the distributor is stuck, seized, no move. The internal weights had seized up too but they free’d off after a good soak with oil. So, the Corsair is looking rather sorry for its self at the moment.
I also took down the distributor I bought some months back and after taking delivery had a suspicion that it was for another Ford car. It is quite different to the one in the Corsair which is probably a Lucas type and the new old stock one I had was a Bosch. Anyway, it was hard to identify the numbers on the box but John knows a man that can and if isn’t suitable then I should have the right info to re-sell it.
I got to have a chat with John (and Peter) from AJ Restorations earlier in the week about the Corsair running problems. It has been suggested that the fault could be a burnt out valve (inlet?) causing the back fire and poor running under load. So John will be picking up the Corsair next week to take back to his workshop to run some tests and potentially fix.
As a result, it spurred me on to finish the front valance that John repaired last year. Well, I couldn’t let the car go back having not done as John suggested last September! So over a couple of days I rubbed the filler primer down with 240, 600 and 800 grit wet and dry paper. Then with an acrylic aerosol bought a few months back sprayed over the primer – unfortunately the colour I chose wasn’t a great match (a bit bright) but should at least make the front more water proof and easier to keep clean.